lt133
Member
I haven’t been around the board much over the summer, but that’s another issue, I did have a great time at Sebago, looking forward to next year. So here’s the problem in a nutshell. I experienced a sudden power loss while throttling up after a 30-minute cruise through a no wake zone. Heard all kinds of bad noises, sounded like drive train. Pulled the motor and found a push rod broke through the rocker arm #2 cylinder exhaust. Further invest showed a couple of valve seals lying in the head on the port side also. There was no other damage, pistons, valves, everything else looks good. There is absolutely no sign of any water or fluids in the cylinder. Any ideas on what would have caused this? People I purchased the motor from don’t want to cover it under warranty telling me it was not a factory defect and that I must have reverted some water and that was my problem, which is definitely not the case. The motor is a stock 502; cam has been changed (don’t have the specs in front of me but it’s somewhere around 561 lift, 114 LSA nothing radical) Hardin Marine XS Extreme intake, Holley 800cfm, Gil Offshore exhaust. My plan for right now (budget restrictions considered) to get back up and running is to replace the stock rocker studs with the Comp Cams Adjustable Rocker Conversion Kit and replace all the rockers with the Comp Cams Pro Magnum Rockers as well as all new valve seals. Springs look fine; engine only has about 20 hours on it. Any ideas or suggestions? Thanks in advance.